Woke up early this morning and cleaned the MAF, DISA, ICV and throttle body, and also replaced the lower intake boot (thought that was the culprit of a high pitched squeal when accelerating - after finishing, the squeal has subsided partially but you can still hear it a little when the driver window is down).
Took me about 3 hours total at a leisurely pace. I'm stoked that everything went so smoothly
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